Cessna 150L Safety Record
Complete NTSB accident and incident history. 464 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 13, 1990 | HETTINGER, ND | N11580 | Fatal (2) | destroyed |
THE PILOT'S FAILURE TO MAINTAIN AIRSPEED DURING CLIMBOUT. CONTRIBUTING FACTORS WERE: THE PILOT'S LACK OF RECENT EXPERIENCE, AND THE OVER MAXIMUM GROSS…THE PILOT'S FAILURE TO MAINTAIN AIRSPEED DURING CLIMBOUT. CONTRIBUTING FACTORS WERE: THE PILOT'S LACK OF RECENT EXPERIENCE, AND THE OVER MAXIMUM GROSS WEIGHT CONDITION OF THE AIRCRAFT. |
| Jun 24, 1990 | BLOUNTVILLE, TN | N1408Q | Incident | substantial | THE PILOT'S INACCURATE FUEL CONSUMPTION CALCULATIONS WHICH RESULTED IN FUEL EXHAUSTION. |
| Jun 23, 1990 | TOMBALL, TX | N1792Q | Incident | substantial |
STUDENT PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL AND PROPER ALIGNMENT WITH TIMELY MANNER AFTER A BOUNCED LANDING. A FACTOR IN THE ACCIDENT WAS …STUDENT PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL AND PROPER ALIGNMENT WITH TIMELY MANNER AFTER A BOUNCED LANDING. A FACTOR IN THE ACCIDENT WAS THE PRESENCE OF A RIGHT QUARTERING HEADWIND. |
| May 08, 1990 | NEWBERG, OR | N18024 | Serious (1) | substantial | THE PILOT DID NOT MAINTAIN DIRECTIONAL CONTROL DUING THE LANDING. |
| May 05, 1990 | STOCKBRIDGE, GA | N10790 | Fatal (1) | destroyed | THE PILOT'S FAILURE TO MAINTAIN THE PROPER CLEARANCE FROM OBJECTS ON THE GROUND. |
| Apr 13, 1990 | HANFORD, CA | N7309G | Incident | substantial | THE FAILURE OF THE PILOT IN COMMAND TO MAINTAIN A SUFFICIENT AIRSPEED FOR THE WIND CONDITIONS ENCOUNTERED DURING THE ATTEMPTED LANDING. |
| Mar 30, 1990 | VIEQUES, PR | N19599 | Incident | substantial |
FAILURE OF PACKING AROUND THE CARBURETOR ACCELERATOR PUMP, WHICH HAD JAMMED THROTTLE MOVEMENT AND WOULD NOT ALLOW AN INCREASE IN ENGINE RPM ABOVE IDLE…FAILURE OF PACKING AROUND THE CARBURETOR ACCELERATOR PUMP, WHICH HAD JAMMED THROTTLE MOVEMENT AND WOULD NOT ALLOW AN INCREASE IN ENGINE RPM ABOVE IDLE. |
| Feb 21, 1990 | ROXBORO, NC | N6845G | Incident | substantial |
THE PILOT'S FAILURE TO USE THE BEFORE LANDING CHECKLIST WHICH REQUIRES THE APPLICATION OF CARBURETOR HEAT. FACTORS WERE SOFT TERRAIN AT ACCIDENT SITE,…THE PILOT'S FAILURE TO USE THE BEFORE LANDING CHECKLIST WHICH REQUIRES THE APPLICATION OF CARBURETOR HEAT. FACTORS WERE SOFT TERRAIN AT ACCIDENT SITE, AND CONDITION FAVORABLE FOR THE FORMATION OF CARBURETOR ICE. |
| Feb 14, 1990 | ARLINGTON, TX | N21969 | Serious (1) | destroyed |
POOR JUDGEMENT OF THE PILOT AFTER CONSUMPTION OF ALCOHOLIC BEVERAGE, HIS DECISION TO MAKE LOW PASSES AT NIGHT (BUZZING), FAILURE OF THE PILOT TO MAINT…POOR JUDGEMENT OF THE PILOT AFTER CONSUMPTION OF ALCOHOLIC BEVERAGE, HIS DECISION TO MAKE LOW PASSES AT NIGHT (BUZZING), FAILURE OF THE PILOT TO MAINTAIN PROPER ALTITUDE, AND DIVERSION OF HIS ATTENTION. DARKNESS WAS A RELATED FACTOR. |
| Feb 10, 1990 | BULLHEAD CITY, AZ | N1272Q | Incident | substantial | THE PILOT'S MISCALCULATION OF THE FUEL REMAINING, WHICH CAUSED THE ENGINE TO QUIT. |
| Jan 08, 1990 | TALLADEGA, AL | N7950F | Serious (1) | destroyed | THE PILOT'S IMPROPER INFLIGHT DECISION TO ATTEMPT TO CONTINUE VFR FLIGHT IMC CONDITIONS WITH NO INSTRUMENT RATING, CLEARANCE OR EXPERIENCE. |
| Jan 07, 1990 | TRAVERSE CITY, MI | N6763G | Incident | substantial | IMPROPER PLANNING/DECISION BY THE PILOT, WHICH RESULTED IN FUEL EXHAUSTION DUE TO AN INADEQUATE SUPPLY OF FUEL. |
| Dec 28, 1989 | LEHIGHTON, PA | N11614 | Incident | substantial | LOSS OF ENGINE POWER FOR AN UNDETERMINED REASON. |
| Oct 25, 1989 | MARANA, AZ | N642EZ | Incident | substantial | FAILURE OF THE PILOT TO PROPERLY JUDGE HIS FUEL SUPPLY, WHICH RESULTED IN FUEL EXHAUSTION. |
| Oct 25, 1989 | COLUMBIA, MS | N19007 | Fatal (1) | destroyed | SUICIDE. THE PILOT'S EMOTIONAL STATE OF DISTRESS WAS A RELATED FACTOR. |
| Sep 28, 1989 | ROCKLEDGE, FL | N17295 | Incident | substantial |
FAILURE OF THE STUDENT PILOT TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRCRAFT, WHICH RESULTED IN AN INADVERTENT GROUND SWERVE. THE GUSTY CROSSWIND A…FAILURE OF THE STUDENT PILOT TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRCRAFT, WHICH RESULTED IN AN INADVERTENT GROUND SWERVE. THE GUSTY CROSSWIND AND PROXIMITY OF THE PARKED AIRCRAFT WERE RELATED FACTORS. |
| Sep 23, 1989 | CARLSBAD, NM | N6633G | Minor | substantial | THE PILOT FAILED TO REFUEL THE AIRPLANE IN A TIMELY MANNER WHICH RESULTED IN FUEL EXHAUSTION. |
| Jul 12, 1989 | DOYLESTOWN, PA | N10659 | Serious (1) | substantial |
IMPROPER PREFLIGHT PREPARATION BY THE PILOT BY TAKING OFF WITH THE FLAPS EXTENDED, WHICH RESULTED IN AN INADEQUATE RATE OF CLIMB TO CLEAR OBSTRUCTIONS…IMPROPER PREFLIGHT PREPARATION BY THE PILOT BY TAKING OFF WITH THE FLAPS EXTENDED, WHICH RESULTED IN AN INADEQUATE RATE OF CLIMB TO CLEAR OBSTRUCTIONS BEYOND THE END OF THE RUNWAY, AND THE PILOT'S DELAY IN ABORTING THE TAKEOFF AND HIS FAILURE IN MAINTAINING AIRSPEED, WHICH REDUCED HIS ABILITY TO FLARE THE AIRCRAFT. THE HIGH OBSTRUCTIONS (TREES) NEAR THE END OF THE RUNWAY WERE CONSIDERED TO BE A FACTOR. |
| Jul 11, 1989 | FORT WORTH, TX | N17250 | Serious (1) | substantial |
A LOSS OF CONTROL OF THE AIRPLANE DUE TO THE PILOT'S INABILITY TO RAISE THE FLAPS WHICH RESULTED IN A STALL. THE FLAP FAILURE AND SUBSEQUENT FULL FLAP…A LOSS OF CONTROL OF THE AIRPLANE DUE TO THE PILOT'S INABILITY TO RAISE THE FLAPS WHICH RESULTED IN A STALL. THE FLAP FAILURE AND SUBSEQUENT FULL FLAP TAKEOFF WERE THE RESULT OF THE OPERATOR'S IMPROPER MAINTENANCE OF THE AIRPLANE AND THE OPERATOR'S USE OF A CUSTOM CHECKLIST THAT DEVIATED SIGNIFICANTLY FROM THE MANUFACTURER'S APPROVED CHECKLIST. CONTRIBUTING TO THE ACCIDENT WERE THE PILOT'S FAILURE TO ENSURE THAT THE FLAPS WERE FULLY RETRACTED PRIOR TO TAKEOFF, AND THE OPERATOR'S INADEQUATE INITIAL TRAINING OF THE PILOT. |
| Jul 02, 1989 | SUGAR GROVE, IL | N16004 | Fatal (1) | destroyed |
FAILURE TO MAINTAIN AIRSPEED ABOVE STALL SPEED, AND A STALL/SPIN ENCOUNTERED WITH INADEQUATE ALTITUDE FOR RECOVERY. FACTORS RELATED TO THE ACCIDENT WE…FAILURE TO MAINTAIN AIRSPEED ABOVE STALL SPEED, AND A STALL/SPIN ENCOUNTERED WITH INADEQUATE ALTITUDE FOR RECOVERY. FACTORS RELATED TO THE ACCIDENT WERE: THUNDERSTORM, PRE-FLIGHT BRIEFING NOT OBTAINED AND POOR WEATHER EVALUATION BY THE PILOT. |
| Jun 18, 1989 | WISC RAPIDS, WI | N6878G | Fatal (1) | destroyed |
THE PILOT'S FAILURE TO ASSURE THAT THE FLAPS WERE IN THE UP POSITION DURING TAKEOFF. A FACTOR RELATED TO THE ACCIDENT WAS THE PILOT'S LACK OF FAMILIAR…THE PILOT'S FAILURE TO ASSURE THAT THE FLAPS WERE IN THE UP POSITION DURING TAKEOFF. A FACTOR RELATED TO THE ACCIDENT WAS THE PILOT'S LACK OF FAMILIARITY WITH AIRCRAFT. |
| May 30, 1989 | JACKSONVILLE, FL | N17018 | Incident | substantial | THE PILOT'S FAILURE TO HAVE SOMEONE OPERATE THE AIRPLANE'S BRAKES AND ENGINE CONTROLS DURING HAND PROPPING THE ENGINE. |
| May 29, 1989 | ONALASKA, TX | N17130 | Incident | substantial |
FUEL SYSTEM EXHAUSTION DUE TO THE IMPROPER PLANNING/DECISION BY THE FLIGHT INSTRUCTOR, ON THE GROUND, PRIOR TO THE FLIGHT AND THE IMPROPER INFLIGHT PL…FUEL SYSTEM EXHAUSTION DUE TO THE IMPROPER PLANNING/DECISION BY THE FLIGHT INSTRUCTOR, ON THE GROUND, PRIOR TO THE FLIGHT AND THE IMPROPER INFLIGHT PLANNING/DECISION BY THE STUDENT PILOT. |
| May 21, 1989 | BAKERSFIELD, CA | N18515 | Minor | substantial |
THE LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION. THE PILOT DID NOT ADEQUATELY PLAN FOR THE FLIGHT IN THAT HE DID NOT CALCULATE THE FUEL CONSUMPTION AC…THE LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION. THE PILOT DID NOT ADEQUATELY PLAN FOR THE FLIGHT IN THAT HE DID NOT CALCULATE THE FUEL CONSUMPTION ACCURATELY, FAILED TO PROVIDE FOR ADEQUATE FUEL RESERVES, AND ALSO FAILED TO LAND AT AIRPORTS SHORT OF HIS DESTINATION EVEN THOUGH HE WAS AWARE OF HIS LOW FUEL STATE. |
| Apr 01, 1989 | BOWLING GREEN, OH | N1044Z | Incident | substantial |
THE STUDENT PILOT FAILED TO MAINTAIN CONTROL OF THE AIRCRAFT WHEN HE MISJUDGED THE HEIGHT OF THE LANDING FLARE. THE RECOVERY FROM THE BOUNCED LANDING …THE STUDENT PILOT FAILED TO MAINTAIN CONTROL OF THE AIRCRAFT WHEN HE MISJUDGED THE HEIGHT OF THE LANDING FLARE. THE RECOVERY FROM THE BOUNCED LANDING WAS INADEQUATE AND THE NOSE GEAR COLLAPSED UPON IMPACT WITH THE RUNWAY. |