Cessna 172 Safety Record
Complete NTSB accident and incident history. 6810 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 14, 1989 | RAVENNA, OH | N4770J | Incident | substantial | FAILURE OF PILOT IN COMMAND TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRPLANE WHILE EXECUTING A TOUCH-AND-GO. |
| Aug 14, 1989 | GRAND TURK ISL., TK | N12634 | Incident | destroyed | Investigation pending |
| Aug 13, 1989 | PASS-A-GRILLE, FL | N99901 | Fatal (4) | destroyed |
FAILURE OF THE PILOT TO RECOVER FROM A STALL/SPIN. EXCESSIVE GROSS WEIGHT OF THE AIRCRAFT AND LACK OF AVAILABLE ALTITUDE FOR SPIN RECOVERY WERE PROBA…FAILURE OF THE PILOT TO RECOVER FROM A STALL/SPIN. EXCESSIVE GROSS WEIGHT OF THE AIRCRAFT AND LACK OF AVAILABLE ALTITUDE FOR SPIN RECOVERY WERE PROBABLE CONTRIBUTING FACTORS. |
| Aug 13, 1989 | REDLANDS, CA | N51920 | Incident | substantial |
THE PILOT'S IMPROPER LEVEL-OFF, RECOVERY FROM BOUNCED LANDING, AND FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING. THE PILOT'S LIMITED REC…THE PILOT'S IMPROPER LEVEL-OFF, RECOVERY FROM BOUNCED LANDING, AND FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING. THE PILOT'S LIMITED RECENT EXPERIENCE WAS A CONTRIBUTING FACTOR. |
| Aug 13, 1989 | SELIGMAN, AZ | N5961J | Minor | substantial |
A LOSS OF ENGINE POWER DUE TO A FAILURE OF THE NUMBER 3 CYLINDER EXHAUST VALVE ROCKER ARM PIVOT STUD, WHICH WAS IN TURN CAUSED BY A STUCK EXHAUST VALV…A LOSS OF ENGINE POWER DUE TO A FAILURE OF THE NUMBER 3 CYLINDER EXHAUST VALVE ROCKER ARM PIVOT STUD, WHICH WAS IN TURN CAUSED BY A STUCK EXHAUST VALVE. |
| Aug 06, 1989 | DANA POINT, CA | N2667L | Fatal (1) | destroyed | PILOT-IN-COMMANDS FAILURE TO MAINTAIN CONTROL OF THE AIRPLANE WHILE IN MANEUVERING FLIGHT. |
| Aug 06, 1989 | ALBUQUERQUE, NM | N64263 | Fatal (1) | destroyed | THE PILOT DELIBERATELY FLEW HIS AIRCRAFT INTO THE FACE OF A MOUNTAIN. A CONTRIBUTING FACTOR WAS: THE PSYCHOLOGICAL CONDITION OF THE PILOT. |
| Aug 05, 1989 | MCKINNEY, TX | N4377L | Incident | substantial | TOTAL FAILURE OF THE ENGINE ASSEMBLY/ROCKER ARM/TAPPET SHAFT. |
| Aug 05, 1989 | RUIDOSO, NM | N9183H | Minor | destroyed |
THE PILOT'S IMPROPER USE OF THE MIXTURE CONTROL AND CARBURETOR HEAT DURING A TAKEOFF IN HIGH DENSITY ALTITUDE CONDITIONS. CONTRIBUTING TO THE ACCIDENT…THE PILOT'S IMPROPER USE OF THE MIXTURE CONTROL AND CARBURETOR HEAT DURING A TAKEOFF IN HIGH DENSITY ALTITUDE CONDITIONS. CONTRIBUTING TO THE ACCIDENT WAS THE HIGH DENSITY ALTITUDE. |
| Aug 03, 1989 | APALACHICOLA, FL | N64RF | Minor | destroyed |
FAILURE OF THE PILOT TO MAINTAIN PROPER ALTITUDE. A FACTOR RELATED TO THE ACCIDENT WAS: THE PILOT'S LACK OF VISUAL PERCEPTION CONCERNING ALTITUDE AB…FAILURE OF THE PILOT TO MAINTAIN PROPER ALTITUDE. A FACTOR RELATED TO THE ACCIDENT WAS: THE PILOT'S LACK OF VISUAL PERCEPTION CONCERNING ALTITUDE ABOVE THE WATER. |
| Aug 02, 1989 | NEWBURGH, NY | N1983F | Incident | substantial |
THE DUAL STUDENT'S MISJUDGEMENT OF THE AIRPLANE'S ALTITUDE AND SPEED DURING THE FLARE FOR LANDING, AND THE IMPROPER USE OF POWER DURING THE FLARE. IN …THE DUAL STUDENT'S MISJUDGEMENT OF THE AIRPLANE'S ALTITUDE AND SPEED DURING THE FLARE FOR LANDING, AND THE IMPROPER USE OF POWER DURING THE FLARE. IN ADDITION, THE CFI FAILED TO ADEQUATELY SUPERVISE THE DUAL STUDENT'S ACTION. |
| Aug 01, 1989 | N MYRTLE BEACH, SC | N336AF | Incident | substantial |
WATER CONTAMINATION OF THE AIRPLANE FUEL SUPPLY, AND THE PILOT'S FAILURE TO ADEQUATELY PREFLIGHT THE AIRCRAFT. A FACTOR RELATED TO THE ACCIDENT WAS: …WATER CONTAMINATION OF THE AIRPLANE FUEL SUPPLY, AND THE PILOT'S FAILURE TO ADEQUATELY PREFLIGHT THE AIRCRAFT. A FACTOR RELATED TO THE ACCIDENT WAS: SWAMPY TERRAIN AT THE EMERGENCY LANDING SITE. |
| Jul 30, 1989 | YERINGTON, NV | N14454 | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN ADEQUATE AIRSPEED DURING A LANDING GO-AROUND IN HIGH DENSITY ALTITUDE CONDITIONS. |
| Jul 29, 1989 | CARSON CITY, NV | N9598H | Incident | substantial |
THE STUDENT PILOT'S IMPROPER COMPENSATION FOR WIND CONDITIONS, AND IMPROPER RECOVERY FROM A BOUNCED LANDING. FACTORS RELATED TO THE ACCIDENT WERE: T…THE STUDENT PILOT'S IMPROPER COMPENSATION FOR WIND CONDITIONS, AND IMPROPER RECOVERY FROM A BOUNCED LANDING. FACTORS RELATED TO THE ACCIDENT WERE: THE ADVERSE WIND CONDITION AND THE STUDENT'S LACK OF TOTAL FLYING EXPERIENCE. |
| Jul 29, 1989 | MT PLEASANT, PA | N19652 | Incident | substantial | AN IMPROPER FLARE BY THE PILOT THAT RESULTED IN A HARD LANDING. |
| Jul 28, 1989 | MARANA, AZ | N61552 | Incident | substantial |
INADEQUATE PREFLIGHT BY THE STUDENT PILOT, INADEQUATE SUPERVISION BY THE FLIGHT INSTRUCTOR (CFI), AND FUEL EXHAUSTION DUE TO LACK OF FUEL. RELATED FA…INADEQUATE PREFLIGHT BY THE STUDENT PILOT, INADEQUATE SUPERVISION BY THE FLIGHT INSTRUCTOR (CFI), AND FUEL EXHAUSTION DUE TO LACK OF FUEL. RELATED FACTORS WERE: INOPERATIVE LEFT FUEL QUANTITY GAGE, THE CFI'S DECISION TO MAKE THE FLIGHT WITH A KNOWN DEFICIENCY IN THE FUEL GAGE, AND OBSTRUCTIONS (TREE LIKE CACTUS) IN THE EMERGENCY LANDING AREA. |
| Jul 27, 1989 | WIXOM, MI | N12662 | Incident | substantial |
CARBURETOR ICE DUE TO THE PILOT'S IMPROPER USE OF CARBURETOR HEAT. FACTORS RELATED TO THE ACCIDENT WERE: WEATHER CONDITIONS CONDUCIVE TO CARBURETOR I…CARBURETOR ICE DUE TO THE PILOT'S IMPROPER USE OF CARBURETOR HEAT. FACTORS RELATED TO THE ACCIDENT WERE: WEATHER CONDITIONS CONDUCIVE TO CARBURETOR ICE, DARK NIGHT, AND TREE(S) IN THE EMERGENCY LANDING AREA. |
| Jul 27, 1989 | WILMINGTON, NC | N7444G | Incident | substantial |
THE INADEQUATE PREFLIGHT PREPARATION/PLANNING BY THE PILOT REGARDING THE UNIQUE LIGHT FEATURES ON RUNWAY 18 (LIGHTS MOUNTED ALONG THE EAST SIDE ONLY).…THE INADEQUATE PREFLIGHT PREPARATION/PLANNING BY THE PILOT REGARDING THE UNIQUE LIGHT FEATURES ON RUNWAY 18 (LIGHTS MOUNTED ALONG THE EAST SIDE ONLY). IN ADDITION THE PILOT FAILED TO ALIGN THE AIRPLANE WITH THE RUNWAY AND STRUCK A VEHICLE THAT WAS PARKED BETWEEN THE LIGHTS. |
| Jul 25, 1989 | GAINESVILLE, FL | N5186J | Incident | substantial |
THE STUDENT'S IMPROPER FLARE FOR LANDING. THE CROSSWIND (QUARTERING HEADWIND) AND THE STUDENT'S LACK OF EXPERIENCE IN THIS AIRCRAFT WERE CONSIDERED T…THE STUDENT'S IMPROPER FLARE FOR LANDING. THE CROSSWIND (QUARTERING HEADWIND) AND THE STUDENT'S LACK OF EXPERIENCE IN THIS AIRCRAFT WERE CONSIDERED TO BE CONTRIBUTING FACTORS. |
| Jul 23, 1989 | DULUTH, MN | N97984 | Incident | substantial | AIRCRAFT CONTROL WAS NOT MAINTAINED BY THE PILOT IN COMMAND DUE TO IMPROPER USE OF THE AIRCRAFT FLIGHT CONTROLS. |
| Jul 22, 1989 | CINCINNATI, OH | N52896 | Incident | substantial |
THE PILOT'S IMPROPER GO-AROUND PROCEDURE OF FULLY RETRACTING THE FLAPS WHICH RESULTED IN THE AIRPLANE MUSHING INTO TREES. CONTRIBUTING FACTOR(S) WAS: …THE PILOT'S IMPROPER GO-AROUND PROCEDURE OF FULLY RETRACTING THE FLAPS WHICH RESULTED IN THE AIRPLANE MUSHING INTO TREES. CONTRIBUTING FACTOR(S) WAS: A MISJUDGEMENT OF FLARE HEIGHT ABOVE THE RUNWAY AND FAILURE TO REMOVE THE CARBURETOR HEAT WHICH MAY HAVE PREVENTED THE AVAILABILITY OF FULL POWER. |
| Jul 20, 1989 | RIDGELAND, SC | N4254L | Fatal (3) | destroyed |
IMPROPER PLANNING/DECISION BY THE PILOT-IN-COMMAND (PIC), WHICH RESULTED IN AN INADVERTENT STALL DURING TAKEOFF. FACTORS RELATED TO THE ACCIDENT WERE…IMPROPER PLANNING/DECISION BY THE PILOT-IN-COMMAND (PIC), WHICH RESULTED IN AN INADVERTENT STALL DURING TAKEOFF. FACTORS RELATED TO THE ACCIDENT WERE: THE EXCESSIVE GROSS WEIGHT AND IMPROPER LIFT-OFF BY THE PIC, THE PILOT/PASSENGER'S IMPROPER CREW COORDINATION REGARDING THE SPECIFIC INSTRUCTIONS THAT HE RECEIVED CONCERNING THE PAYLOAD LIMITATIONS, AND THE HIGH DENSITY ALTITUDE. |
| Jul 19, 1989 | LEESBURG, FL | N47ER | Minor | substantial | FAILURE OF THE PILOT TO MAINTAIN ADEQUATE AIRSPEED, WHICH RESULTED IN AN INADVERTENT STALL AS HE INITIATED A GO-AROUND. |
| Jul 13, 1989 | FOREST, MS | N3905L | Serious (1) | substantial |
FAILURE OF THE PILOT TO MAINTAIN RUNWAY ALIGNMENT AND PARTIAL LOSS OF POWER FROM WATER IN THE FUEL. CONTRIBUTING FACTORS WERE: UNEVEN RUNWAY, PILOT'…FAILURE OF THE PILOT TO MAINTAIN RUNWAY ALIGNMENT AND PARTIAL LOSS OF POWER FROM WATER IN THE FUEL. CONTRIBUTING FACTORS WERE: UNEVEN RUNWAY, PILOT'S IMPROPER RECOVERY FROM A BOUNCED LANDING, A GUSTY CROSSWIND CONDITION, AND TREES. |
| Jul 12, 1989 | HATTON, ND | N3269L | Minor | destroyed |
IMPROPER IN-FLIGHT PLANNING/DECISION BY THE PILOT AND HIS FAILURE TO MAINTAIN SUFFICIENT CLEARANCE ABOVE THE GROUND. THE TAILWIND, HIGH OBSTRUCTION (S…IMPROPER IN-FLIGHT PLANNING/DECISION BY THE PILOT AND HIS FAILURE TO MAINTAIN SUFFICIENT CLEARANCE ABOVE THE GROUND. THE TAILWIND, HIGH OBSTRUCTION (SHELTER BELT), AND DOWNDRAFT WERE CONTRIBUTING FACTORS. |