Cessna 177 Safety Record
Complete NTSB accident and incident history. 766 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 17, 1995 | MIAMI, FL | N3470T | Incident | substantial |
The pilot-in-command's/CFI improper supervision of the dual student during a simulated short field approach for landing. This resulted in an in-flight…The pilot-in-command's/CFI improper supervision of the dual student during a simulated short field approach for landing. This resulted in an in-flight loss of control (inadvertent stall), and subsequent hard landing. |
| Feb 20, 1995 | TERLINGUA, TX | N34958 | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL. FACTORS WERE HIS DECISION TO LAND ON THE UNLIT RUNWAY AND THE DUSK LIGHT CONDITIONS. |
| Feb 04, 1995 | CORVALLIS, OR | N2901X | Incident | substantial | THE PILOT'S IMPROPER FLARE AND IMPROPER RECOVERY FROM A BOUNCED LANDING. |
| Jan 01, 1995 | TORREON, NM | N30898 | Incident | substantial |
THE PILOT'S FAILURE TO ATTAIN PROPER LIFTOFF SPEED RESULTING IN AN INADVERTENT STALL AND THE FAILURE TO REMOVE FROST FROM THE WING. A FACTOR WAS FATIG…THE PILOT'S FAILURE TO ATTAIN PROPER LIFTOFF SPEED RESULTING IN AN INADVERTENT STALL AND THE FAILURE TO REMOVE FROST FROM THE WING. A FACTOR WAS FATIGUE. |
| Dec 04, 1994 | KATY, TX | N29400 | Incident | substantial | FUEL EXHAUSTION DUE TO THE PILOT'S FAILURE TO REFUEL. A FACTOR WAS THE UNSUITABLE TERRAIN AT THE PILOT'S DISPOSAL FOR THE FORCED LANDING. |
| Oct 15, 1994 | LAYTONVILLE, CA | N7577V | Incident | substantial | were the pilot's failure to maintain the proper airspeed and attain the proper touchdown point. |
| Jul 17, 1994 | ROTA ISLAND, PO | N1423C | Incident | substantial | THE PILOT'S PORPOISING THE AIRCRAFT UPON LANDING AND HIS INADEQUATE RECOVERY FROM A BOUNCED LANDING. |
| Jun 13, 1994 | WATONGA, OK | N2867X | Incident | substantial |
WAS THE PILOT'S FAILURE TO MAINTAIN THE PROPER GLIDEPATH, HIS FAILURE TO COMPENSATE FOR EXISTING WIND CONDITIONS, AND HIS FAILURE TO MAINTAIN CLEARANC…WAS THE PILOT'S FAILURE TO MAINTAIN THE PROPER GLIDEPATH, HIS FAILURE TO COMPENSATE FOR EXISTING WIND CONDITIONS, AND HIS FAILURE TO MAINTAIN CLEARANCE WITH THE FENCE. A FACTOR WAS THE WEATHER. |
| Apr 05, 1994 | SEDONA, AZ | N35060 | Incident | substantial | the pilot's inadequate compensation of the existing wind conditions, and failure to maintain directional control of the aircraft. |
| Mar 31, 1994 | CHARLOTTE, MI | N7581V | Incident | substantial | the deer which ran onto the runway. Factors related to the accident were the night conditions and the runway lights which were contacted. |
| Dec 07, 1993 | SANTA MONICA, CA | N52039 | Incident | substantial | THE PILOT'S FAILURE TO ATTAIN THE PROPER TOUCHDOWN POINT AND IMPROPER RECOVERY FROM A BOUNCED LANDING. |
| Oct 28, 1993 | PLEASANT GROVE, CA | N18174 | Incident | substantial | THE FAILURE OF THE STARTER TO TURN THE ENGINE OVER DUE TO INADEQUATE MAINTENANCE AND INSPECTION. |
| Oct 04, 1993 | LA SAL, UT | N30365 | Incident | substantial | THE PILOT IN COMMAND'S FAILURE TO ABORT THE TAKEOFF. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE HIGH (10,000 FOOT) DENSITY ALTITUDE AND THE FENCE. |
| Sep 27, 1993 | FAYETTE, IA | N35163 | Incident | substantial | the pilot-in-command's failure to refuel the airplane. A factor was a road sign and fuel exhaustion. |
| Sep 10, 1993 | VALDOSTA, GA | N2074Q | Incident | substantial |
THE PILOT'S INADEQUATE EVALUATION OF INFLIGHT WEATHER CONDITIONS WHICH RESULTED IN THE INFLIGHT ENCOUNTER WITH SEVERE TURBULENCE AND SUBSEQUENT OVERST…THE PILOT'S INADEQUATE EVALUATION OF INFLIGHT WEATHER CONDITIONS WHICH RESULTED IN THE INFLIGHT ENCOUNTER WITH SEVERE TURBULENCE AND SUBSEQUENT OVERSTRESS OF THE AIRFRAME. |
| Aug 28, 1993 | CAMERON PARK, CA | N33195 | Incident | substantial |
THE PILOT'S FAILURE TO ASSURE THAT THE LANDING GEAR WAS DOWN AND LOCKED. FACTORS RELATING TO THIS ACCIDENT WERE THE ALTERNATOR FAILURE DUE TO A BROKEN…THE PILOT'S FAILURE TO ASSURE THAT THE LANDING GEAR WAS DOWN AND LOCKED. FACTORS RELATING TO THIS ACCIDENT WERE THE ALTERNATOR FAILURE DUE TO A BROKEN WIRE AND THE LOW BATTERY OUTPUT. |
| Aug 16, 1993 | HOUSTON, TX | N34689 | Incident | substantial |
ENGINE POWER LOSS DUE TO FUEL EXHAUSTION FOR UNDETERMINED REASONS. FACTORS WERE THE PILOT'S FAILURE TO MONITOR AND RECALCULATE FUEL CONSUMPTION EN ROU…ENGINE POWER LOSS DUE TO FUEL EXHAUSTION FOR UNDETERMINED REASONS. FACTORS WERE THE PILOT'S FAILURE TO MONITOR AND RECALCULATE FUEL CONSUMPTION EN ROUTE AND THE LACK OF SUITABLE TERRAIN ONTO WHICH THE FORCED LANDING COULD HAVE BEEN EXECUTED. |
| Aug 09, 1993 | GRAND PRAIRIE, TX | N34293 | Incident | substantial |
LOSS OF ENGINE POWER DUE TO FUEL STARVATION AS A RESULT OF A LEAKING FUEL LINE. THE FUEL LINE WAS NOT THE CORRECT PART AS A RESULT OF A MISIDENTIFICAT…LOSS OF ENGINE POWER DUE TO FUEL STARVATION AS A RESULT OF A LEAKING FUEL LINE. THE FUEL LINE WAS NOT THE CORRECT PART AS A RESULT OF A MISIDENTIFICATION BY CESSNA. |
| Aug 04, 1993 | EMPORIA, KS | N33299 | Incident | substantial | THE PILOT'S SELECTION OF UNSUITABLE TERRAIN. |
| Jul 26, 1993 | COLUMBUS, IN | N1850Q | Incident | substantial |
the pilot in command's failure to maintain proper clearance. A factor involved in this accident is the pilot in command's failure to maintain a prope…the pilot in command's failure to maintain proper clearance. A factor involved in this accident is the pilot in command's failure to maintain a proper glidepath. |
| Jul 05, 1993 | ATLANTA, GA | N29499 | Incident | substantial | The failure of the pilot to maintain directional control of the aircraft. |
| Jul 04, 1993 | SHAWNEE, OK | N18739 | Incident | substantial | FUEL SYSTEM EXHAUSTION INDUCED POWER LOSS FOR UNDETERMINED REASONS. A FACTOR WAS A LACK OF SUITABLE TERRAIN. |
| Jul 03, 1993 | AKRON, CO | N30248 | Incident | substantial |
THE PILOT'S INADEQUATE COMPENSATION FOR WIND CONDITIONS. FACTORS WERE: THE PILOT'S FAILURE TO INITIATE A GO AROUND IN A MORE TIMELY MANNER, AND GUSTY…THE PILOT'S INADEQUATE COMPENSATION FOR WIND CONDITIONS. FACTORS WERE: THE PILOT'S FAILURE TO INITIATE A GO AROUND IN A MORE TIMELY MANNER, AND GUSTY CROSSWINDS. |
| May 31, 1993 | NEWPORT, NH | N30041 | Incident | substantial | THE PILOT'S FAILURE TO PROPERLY RECOVER FROM A BOUNCED LANDING, AND HIS FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE ABORTED LANDING. |
| Apr 07, 1993 | BROOKVILLE, OH | N11828 | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL. CONTRIBUTING WAS THE LACK OF RECENCY OF EXPERIENCE. |