Cessna 421 Safety Record
Complete NTSB accident and incident history. 326 events recorded from 1982 to 2024.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 17, 2001 | New Braunfels, TX | N5286Z | Incident | substantial | the pilot's inadequate flare of the airplane resulting in a hard landing. A contributing factor was the crosswind. |
| May 29, 2001 | Greenville, MS | N51ER | Incident | substantial |
The improper installation by maintenance personnel of the push-pull rod assembly on the right elevator trim tab horn resulted in an in-flight separati…The improper installation by maintenance personnel of the push-pull rod assembly on the right elevator trim tab horn resulted in an in-flight separation of the right elevator trim tab. |
| May 09, 2001 | Angwin, CA | N26560 | Minor | substantial | Right main landing gear brake lockup during landing rollout for undetermined reasons. |
| Feb 14, 2001 | Munford, AL | N5AY | Fatal (5) | destroyed |
The pilot continued visual flight into instrument weather conditions that resulted in the inflight collision with a river bank. Factors were reduced v…The pilot continued visual flight into instrument weather conditions that resulted in the inflight collision with a river bank. Factors were reduced visibility and dark night. |
| Dec 14, 2000 | PENSACOLA, FL | N781SL | Incident | substantial |
The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the acciden…The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the accident was the failure of unknown maintenance personnel to comply with a manufacturers service letter concerning the scissors washers. |
| Dec 10, 2000 | NORMAN, OK | N52KL | Fatal (2) | destroyed |
the pilot's failure to follow the instrument approach procedure and his continued descent below the prescribed minimum descent altitude (MDA). Contri…the pilot's failure to follow the instrument approach procedure and his continued descent below the prescribed minimum descent altitude (MDA). Contributory factors were the pilot's physical impairment from drugs, the low ceiling, fog, and dark night light conditions. |
| Aug 24, 2000 | HUNT, TX | N421NT | Fatal (1) | destroyed |
the loss of left engine power as a result of the owner's failure to overhaul the engine before further flight after the lubrication system was found c…the loss of left engine power as a result of the owner's failure to overhaul the engine before further flight after the lubrication system was found contaminated with metal. Contributing factors were the pilot's decision to fly the aircraft with a non-operating landing gear system, which resulted in a forced landing, and the lack of suitable terrain for the forced landing. |
| Jul 25, 2000 | HOMEWOOD, MS | N1477D | Incident | substantial |
The inadequate installation of the right propeller by the mechanic for his failure to properly torque the eight nuts resulting in fatigue failure of t…The inadequate installation of the right propeller by the mechanic for his failure to properly torque the eight nuts resulting in fatigue failure of the studs and separation of the right propeller during cruise flight. Findings in the investigation were 1) the mechanic who installed the right propeller used un-calibrated torque wrenches, and 2) the mechanic who installed the right propeller used an outdated Service Manual. |
| Jan 02, 2000 | TELLURIDE, CO | N421CF | Fatal (1) | destroyed |
The non-instrument rated pilot's intentional flight into IMC, and his subsequent spatial disorientation that resulted in an inadvertent stall. A fact…The non-instrument rated pilot's intentional flight into IMC, and his subsequent spatial disorientation that resulted in an inadvertent stall. A factor was the snow showers weather condition. |
| Dec 11, 1999 | GILLETTE, WY | N3912C | Incident | substantial | The collision with a deer on the runway during a night landing. A factor was the dark night. |
| Oct 05, 1999 | MONTAGUE, CA | N69GP | Incident | substantial |
The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional cont…The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional control. |
| Sep 23, 1999 | SANTA MONICA, CA | N26585 | Minor | substantial |
The failure of the pilot to establish and maintain a stabilized approach, which resulted in a hard landing and on-ground collision with the airport VA…The failure of the pilot to establish and maintain a stabilized approach, which resulted in a hard landing and on-ground collision with the airport VASI display. |
| Jul 02, 1999 | POLACCA, AZ | N5943M | Minor | substantial |
The pilot's inadequate preflight inspection, which failed to determine the fuel supply in each fuel tank, and his mismanagement of the fuel supply, wh…The pilot's inadequate preflight inspection, which failed to determine the fuel supply in each fuel tank, and his mismanagement of the fuel supply, which resulted in fuel starvation. |
| Jun 14, 1999 | CHARLOTTE, NC | N421LL | Fatal (4) | destroyed |
The failure of the pilot to shutdown the right engine and feather the propeller after a reported loss of power in the engine shortly after takeoff res…The failure of the pilot to shutdown the right engine and feather the propeller after a reported loss of power in the engine shortly after takeoff resulting in the airplane descending, colliding with trees and then the ground. |
| May 27, 1999 | JEFFERSON CITY, MO | N34TM | Fatal (4) | destroyed | the pilot failed to maintain control of the airplane. A factor was the partial loss of power due to the exhaust valve fatigue failure. |
| Mar 09, 1999 | NORTH BEND, OR | N41096 | Fatal (2) | substantial | A delayed aborted takeoff for an undetermined reason. |
| Jan 15, 1999 | YOUNGSTOWN, OH | N882BB | Incident | substantial | The pilot's failure to maintain aircraft control. A factor was the icy runway. |
| Jan 01, 1999 | SHELBYVILLE, TX | N234CG | Minor | substantial |
The total failure of the aircraft's electrical system. Factors were the thunderstorms, the dusk light condition, and the lack of suitable terrain for…The total failure of the aircraft's electrical system. Factors were the thunderstorms, the dusk light condition, and the lack of suitable terrain for the precautionary landing. |
| Oct 18, 1998 | EAGLE PASS, TX | N19MH | Minor | destroyed | A downdraft, which exceeded the aircraft's climb performance. A factor was the thunderstorms in the vicinity of the airport. |
| Aug 06, 1998 | COLUMBUS, IN | N5MJ | Serious (2) | substantial |
the pilot-in-commands failure to maintain airspeed and the subsequent stall/mush. Factors associated with the accident were the open baggage door and…the pilot-in-commands failure to maintain airspeed and the subsequent stall/mush. Factors associated with the accident were the open baggage door and the inadequate aircraft preflight. |
| Jun 01, 1998 | LITTLE FALLS, MN | N541N | Fatal (1) | destroyed | the pilot's continued operation with a known deficiency in equipment. |
| May 11, 1998 | NASSAU, BF | N17BN | Serious (1) | substantial | Investigation pending |
| Mar 18, 1998 | SHOW LOW, AZ | N70PD | Incident | substantial | The pilot's failure to attain the proper alignment on the runway due to the obscuration by snow of the runway and on the airplane's windows. |
| Dec 28, 1997 | ELKINS, WV | N1348T | Minor | destroyed |
The flight instructor's failure to identify an unsafe runway condition and his delay in aborting the takeoff. Contributing was the aircraft's maximum …The flight instructor's failure to identify an unsafe runway condition and his delay in aborting the takeoff. Contributing was the aircraft's maximum takeoff weight exceeded, and a snow-covered runway. |
| Nov 07, 1997 | TOMAHAWK, WI | N2957Q | Incident | substantial |
the elevator trim tab bolt backed out, allowing the trim tab to flutter, and destroy the elevator. The factors involved were improper annual inspecti…the elevator trim tab bolt backed out, allowing the trim tab to flutter, and destroy the elevator. The factors involved were improper annual inspection by the maintenance personnel, and the inadequate aircraft preflight done by the pilot. |