Boeing 737 Safety Record
Complete NTSB accident and incident history. 1188 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 15, 1997 | ONTARIO, CA | N956UA | Incident | — | a laser light source of undetermined origin directed toward the cockpit window of an aircraft in-flight by a person or persons unknown. |
| Jun 20, 1997 | COPENHAGEN, DA | EI-CDT | Incident | — | Investigation pending |
| May 11, 1997 | CORPUS CHRISTI, TX | N16618 | Incident | — |
The flightcrew's inadequate in-flight planning and decision, and their failure to refer to the navaids needed for the instrument approach procedure. …The flightcrew's inadequate in-flight planning and decision, and their failure to refer to the navaids needed for the instrument approach procedure. A factor was the lack of a minimum safe altitude warning from approach control. |
| Apr 17, 1997 | COLORADO SPGS, CO | N962WP | Incident | — | An oil leak around the APU aft bearing seal which resulted in a fire in the APU exhaust. |
| May 11, 1996 | DALLAS, TX | N315SW | Incident | minor |
failure of the pilot to maintain directional control and runway alignment, during the landing roll out. Factors relating to the incident were: darkne…failure of the pilot to maintain directional control and runway alignment, during the landing roll out. Factors relating to the incident were: darkness, the adverse weather condition, the wet runway, and reduced visibility due to the inadvertent encounter with heavy rain. |
| Apr 30, 1996 | ONTARIO, CA | N331SW | Incident | minor | The repair facility's improper assembly of the landing gear oleo strut during overhaul. |
| Mar 21, 1996 | JACKSONVILLE, FL | EICLK | Incident | substantial |
failure of the nose gear taxi light support bracket due to in service damage, which resulted in debris being ingested by the engines. Contributing to …failure of the nose gear taxi light support bracket due to in service damage, which resulted in debris being ingested by the engines. Contributing to the accident was the failure of company maintenance personnel to comply with a Grimes Service Bulletin and a Boeing Service Letter which recommended changing the nose gear taxi light support bracket to an improved design. |
| Feb 20, 1996 | WASHINGTON, DC | N33202 | Incident | minor |
excessive airspeed was maintained by the captain during the approach/landing phase of the flight, which resulted in an overrun and an encounter with s…excessive airspeed was maintained by the captain during the approach/landing phase of the flight, which resulted in an overrun and an encounter with soft/wet terrain. Factors relating to the incident were: the pilot's failure to attain the proper touchdown point, the wet runway condition, and partial failure of the anti-skid brake system. |
| Dec 29, 1995 | ATLANTA, GA | N306DL | Incident | substantial | Failure of the tug driver, who was towing the Lockheed L-1011, to ensure that clearance was maintained from the Boeing 737, which was standing. |
| Nov 02, 1995 | PORTLAND, ME | N373US | Incident | minor | a bird strike during takeoff, which resulted in failure of several fan blades in the right engine and a partial loss of engine power. |
| Sep 06, 1995 | MIAMI, FL | N405KW | Incident | substantial | IMPROPER PLANNING/DECISION BY THE COMPANY DRIVER OF THE VEHICLE (PAYMOVER) AND UNCOMMANDED MOVEMENT OF THE PAYMOVER FOR UNDETERMINED REASONS. |
| Aug 25, 1995 | FORT LAUDERDALE, FL | N373US | Incident | — | LOW ELECTRICAL RESISTANCE OF THE AUTOPILOT AILERON ACTUATOR FOR UNSPECIFIED REASONS WHICH RESULTED IN AN UNCOMMANDED ROLL TO THE RIGHT. |
| Aug 18, 1995 | LUBBOCK, TX | N309SW | Incident | minor |
installation of an incorrect bearing in the number three main wheel by the wheel assembly supplier, which led to subsequent failure of the wheel beari…installation of an incorrect bearing in the number three main wheel by the wheel assembly supplier, which led to subsequent failure of the wheel bearing and separation of the wheel during takeoff. |
| Aug 05, 1995 | CHARLOTTE, NC | N396US | Incident | — |
IMPROPER INSTALLATION OF THE 'A' SYSTEM FLIGHT CONTROL COMPUTER BY COMPANY MAINTENANCE PERSONNEL, WHICH RESULTED IN PIN CONNECTOR(S) BEING PUSHED LOOS…IMPROPER INSTALLATION OF THE 'A' SYSTEM FLIGHT CONTROL COMPUTER BY COMPANY MAINTENANCE PERSONNEL, WHICH RESULTED IN PIN CONNECTOR(S) BEING PUSHED LOOSE AND SUBSEQUENT MALFUNCTION OF THE AUTOPILOT. |
| Jul 28, 1995 | DALLAS, TX | N675AA | Incident | substantial |
FAILURE OF THE FLIGHTCREWS OF THE BOEING 737, N675AA, AND THE CESSNA 401, N31DB, TO SEE AND AVOID EACH OTHER. FACTORS WERE: THE FAILURE OF 737 FLIGHTC…FAILURE OF THE FLIGHTCREWS OF THE BOEING 737, N675AA, AND THE CESSNA 401, N31DB, TO SEE AND AVOID EACH OTHER. FACTORS WERE: THE FAILURE OF 737 FLIGHTCREW TO RESPOND TO THE TRAFFIC ADVISORY GIVEN BY THE GROUND CONTROLLER IDENTIFYING POTENTIALLY CONFLICTING TRAFFIC, AND THE FAILURE OF THE GROUND CONTROLLER TO ISSUE SEQUENCING INSTRUCTIONS TO BOTH AIRCRAFT. |
| Jul 18, 1995 | ORLANDO, FL | N390US | Incident | — |
CONTAMINATION OF THE WIRING HARNESS AND ELECTRICAL CONNECTORS TO THE E-1-2 AND E-1-3 SHELF DISCONNECT BRACKETS IN THE ELECTRONICS COMPARTMENT, WHICH R…CONTAMINATION OF THE WIRING HARNESS AND ELECTRICAL CONNECTORS TO THE E-1-2 AND E-1-3 SHELF DISCONNECT BRACKETS IN THE ELECTRONICS COMPARTMENT, WHICH RESULTED IN AN ELECTRICAL FAULT AND AN UNCOMMANDED ROLL MALFUNCTION OF THE AUTOPILOT. A FACTOR RELATING TO THE INCIDENT WAS: INADEQUATE MAINTENANCE INSPECTION OF THE AIRCRAFT BY COMPANY MAINTENANCE PERSONNEL. |
| Jun 29, 1995 | ELKO, NV | N457TM | Incident | minor | in-flight separation of the aileron as a result of inadequate bonding. |
| Apr 14, 1995 | DENVER, CO | EICEU | Incident | substantial |
PROPER DESCENT RATE NOT MAINTAINED BY THE FIRST OFFICER, RESULTING IN A HARD LANDING. FACTORS WERE UNFAVORABLE WIND CONDITIONS AND THE CAPTAIN'S INADE…PROPER DESCENT RATE NOT MAINTAINED BY THE FIRST OFFICER, RESULTING IN A HARD LANDING. FACTORS WERE UNFAVORABLE WIND CONDITIONS AND THE CAPTAIN'S INADEQUATE SUPERVISION OF THE FIRST OFFICER. |
| Apr 07, 1995 | CHICAGO, IL | N9090U | Incident | minor |
the inadequacy or deterioration of lubricating grease in the wheel bearing, which led to the total bearing failure and subsequent loss of the wheel. …the inadequacy or deterioration of lubricating grease in the wheel bearing, which led to the total bearing failure and subsequent loss of the wheel. Factors were the insufficiently defined procedures for repacking the bearing, along with an insufficient method of retaining lubricant within the bearing. |
| Jan 24, 1995 | ALBUQUERQUE, NM | N155AW | Incident | — |
maintenance personnel inadvertently overservicing the left main landing gear strut with nitrogen that, during rotation with the aircraft weight on the…maintenance personnel inadvertently overservicing the left main landing gear strut with nitrogen that, during rotation with the aircraft weight on the strut reduced, gave the pilots a rolling sensation to the right. |
| Jan 19, 1995 | ATLANTA, GA | N4515W | Incident | minor |
THE INADEQUATE INSPECTION OF THE AIRCRAFT BY OTHER MAINTENANCE PERSONNEL, IN THAT THEY DID NOT PROPERLY DIAGNOSE DISCREPANCIES IN THE ANTISKID BRAKING…THE INADEQUATE INSPECTION OF THE AIRCRAFT BY OTHER MAINTENANCE PERSONNEL, IN THAT THEY DID NOT PROPERLY DIAGNOSE DISCREPANCIES IN THE ANTISKID BRAKING SYSTEM. |
| Jan 01, 1995 | HOUSTON, TX | N326SW | Incident | — | ENCOUNTER WITH WAKE TURBULENCE. |
| Feb 10, 1994 | CHICAGO, IL | N408PE | Incident | minor |
AN INADEQUATE PROCEDURE FOR HANDLING OF WHEEL CHOCKS BY COMPANY MAINTENANCE AND OPERATIONS PERSONNEL. FACTORS ASSOCIATED WITH THIS ACCIDENT WERE AN IN…AN INADEQUATE PROCEDURE FOR HANDLING OF WHEEL CHOCKS BY COMPANY MAINTENANCE AND OPERATIONS PERSONNEL. FACTORS ASSOCIATED WITH THIS ACCIDENT WERE AN INADEQUATE INSPECTION OF THE AIRPLANE BY COMPANY MAINTENANCE PERSONNEL, AND AN INADEQUATE PRE-FLIGHT INSPECTION BY THE CO-PILOT. |
| Jan 19, 1994 | LITTLE ROCK, AR | N53SW | Incident | minor | WAS THE LANDING GEAR SEPARATION DUE TO AN UNDETERMINED CAUSE. |
| Dec 08, 1993 | DFW AIRPORT, TX | N166AW | Incident | minor | A FAILURE BY THE PILOT-IN-COMMAND TO ATTAIN A STABILZED APPROACH. FACTORS WERE THE FOG AND FAILURE OF THE COPILOT TO MONITOR THE APPROACH. |