Cessna 172L Safety Record
Complete NTSB accident and incident history. 162 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Nov 16, 2005 | Rock Springs, WY | N2870Q | Incident | substantial | the loss of engine power for reasons undetermined. Contributing to the accident was the dark night and lack of suitable terrain for a forced landing. |
| Nov 08, 2005 | Lehighton, PA | N7684G | Incident | substantial |
The pilot's inadequate preflight inspection, which resulted in a total loss of engine power during takeoff due to fuel contamination, and a subsequent…The pilot's inadequate preflight inspection, which resulted in a total loss of engine power during takeoff due to fuel contamination, and a subsequent forced landing to a field. |
| Jun 26, 2005 | Tangier, VA | N19681 | Incident | substantial | The pilot's failure to maintain directional control during landing. |
| Apr 03, 2005 | Stephenville, TX | N3889Q | Incident | substantial | The pilot's improper recovery from a bounced landing, which resulted in a hard landing. A contributing factor was the prevailing crosswind. |
| Mar 30, 2005 | Chino, CA | N7832G | Incident | substantial | the pilot's inadequate compensation for a gusting crosswind and his failure to maintain directional control. |
| Jan 01, 2005 | Poughkeepsie, NY | N7180Q | Incident | substantial | The pilot's inadequate preflight, which resulted in a loss of engine power due to fuel contamination. |
| Aug 14, 2003 | Harvard, IL | N7054Q | Incident | substantial | The pilot's improper flare which led to a hard landing. |
| Jun 07, 2003 | Newburyport, MA | N7149Q | Incident | substantial | The pilot's failure to attain the proper touchdown point. |
| Oct 11, 2002 | San Antonio, TX | N7616G | Incident | substantial | The pilot's inadequate compensation for wind resulting in a loss of directional control. A contributing factor was the prevailing crosswind. |
| Oct 05, 2002 | Fish Lake, MN | N713SX | Incident | substantial | The altitude/clearance not maintained while maneuvering on short final for landing on the lake. The glassy water was a contributing factor. |
| Mar 07, 2002 | BULLHEAD CITY, AZ | N7774G | Incident | substantial | The pilot's failure to comply with maintenance/inspection requirements that resulted in a propeller failure. |
| Dec 09, 2001 | Reedsburg, WI | N4303Q | Incident | substantial |
The pilot inadvertently released the seat adjustment mechanism which resulted in the seat sliding back during takeoff, and his subsequent failure to m…The pilot inadvertently released the seat adjustment mechanism which resulted in the seat sliding back during takeoff, and his subsequent failure to maintain control of the airplane. A factor associated with the accident was the runway light control box, which the airplane contacted. |
| Oct 17, 2001 | Northampton, MA | N811P | Incident | substantial | The pilots' failure to maintain airspeed, which resulted in a loss of control and a hard landing. |
| Mar 03, 2001 | Fort Lauderdale, FL | N3802Q | Incident | substantial |
The total failure of the yoke weld assembly due to corrosion resulting in the inability of the flight crew to maintain elevator control of the airplan…The total failure of the yoke weld assembly due to corrosion resulting in the inability of the flight crew to maintain elevator control of the airplane. Additionally, inadequate annual inspection of the airplane by other maintenance personnel for failure to identfiy extensive corrosion of the yoke. Findings in the investigation were: 1) The airplane was partially submerged in salt water as a result of hurricane Floyd in September 1999, 2) The Advisory Circulars do not identify inspection procedures what to do in case an airplane is sumberged or partially submerged in salt water, and 3) The airplane manufacturer does not have inspection procedures when an airplane is submerged or partially submerged in salt water. |
| Jan 21, 2001 | Culver, IN | N4378Q | Incident | substantial | the proper glide path not attained by both pilots during a short field landing. The snow bank was a contributing factor. |
| Sep 16, 2000 | EVERETT, WA | N7195Q | Incident | substantial |
The other pilot's improper use (inadvertent release) of the brakes. Contributing factors were, a standing aircraft and the other pilot's diverting hi…The other pilot's improper use (inadvertent release) of the brakes. Contributing factors were, a standing aircraft and the other pilot's diverting his attention from outside his aircraft. |
| Jul 10, 2000 | BEAUFORT, NC | N3875Q | Incident | substantial |
A loss of engine power due to failure of the No. 4 cylinder connecting rod during the first flight following engine overhaul for undetermined reasons.…A loss of engine power due to failure of the No. 4 cylinder connecting rod during the first flight following engine overhaul for undetermined reasons. Contributing to the accident was unsuitable terrain. |
| Mar 10, 2000 | BEAUFORT, NC | N3875Q | Incident | substantial |
The failure of the pilot to initiate a go-around after the airplane began to porpoise, resulting in a hard landing and structural damage to the airpla…The failure of the pilot to initiate a go-around after the airplane began to porpoise, resulting in a hard landing and structural damage to the airplane. |
| Dec 28, 1999 | NEW ORLEANS, LA | N172GT | Incident | substantial |
The pilot's inadvertent starting of the engine. Factors were the pilot's failure to set the mixture control to the off position, and the intermittent…The pilot's inadvertent starting of the engine. Factors were the pilot's failure to set the mixture control to the off position, and the intermittent short in the starter switch. |
| Dec 08, 1999 | WOOSTER, OH | N7565G | Incident | substantial | The pilot's inadvertent taxi onto unsuitable terrain. A factor was the burnt out landing/taxi light. |
| Jul 14, 1999 | MONTEZUMA, IA | N19752 | Incident | substantial |
the pilot inadvertently landed on the wrong runway and exceeded the proper touchdown point on the runway. Factors associated with the accident were t…the pilot inadvertently landed on the wrong runway and exceeded the proper touchdown point on the runway. Factors associated with the accident were the gusty tailwind, the fence, and the ditch. |
| Jun 16, 1999 | MILLINOCKET, ME | N7897G | Incident | substantial | The total loss of engine power for undetermined reasons. |
| May 25, 1999 | GUNNISON, CO | N172KB | Incident | substantial |
The pilot's inadvertent stall/mush immediately after takeoff. Factors were the high density altitude weather condition, and the pilot's total lack of…The pilot's inadvertent stall/mush immediately after takeoff. Factors were the high density altitude weather condition, and the pilot's total lack of experience in type of operation. |
| Jan 26, 1999 | SANTA PAULA, CA | N7639G | Incident | substantial |
The instructor pilot's misjudged altitude and speed, which resulted in a failure to attain the proper touchdown point causing an overrun and collision…The instructor pilot's misjudged altitude and speed, which resulted in a failure to attain the proper touchdown point causing an overrun and collision with a block wall. A factor was the wet runway, which may have hindered brake effectiveness. |
| Sep 30, 1998 | PUYALLUP, WA | N2880Q | Incident | substantial |
The pilot-in-command's failure to refuel en-route resulting in fuel exhaustion. Contributing factors were a vehicle (in the landing path) and dark nig…The pilot-in-command's failure to refuel en-route resulting in fuel exhaustion. Contributing factors were a vehicle (in the landing path) and dark night conditions. |