Cessna 414 Safety Record

Complete NTSB accident and incident history. 149 events recorded from 1982 to 2026.

149

All Events

59

Incidents

15

Minor

16

Serious

58

Fatal (148 fatalities)

Date Location Reg# Severity Damage Probable Cause
Mar 19, 2004 Midland, TX N414FB Incident minor The in-flight wing fire for undetermined reasons.
May 26, 2003 PORT JEFFERSON, NY N1234 Incident destroyed Loss of power to both engines for undetermined reasons.
Jun 01, 2000 Prescott Valley, AZ N414PS Incident substantial
The pilot's physical impairment due to the cumulative effects of carbon monoxide from engine exhaust by-products, carbon monoxide from heavy tobacco u…

The pilot's physical impairment due to the cumulative effects of carbon monoxide from engine exhaust by-products, carbon monoxide from heavy tobacco use, and the loss of an undetermined amount of cabin pressurization. A factor in the loss of pressurization was a fractured clamp.

Jun 13, 1999 SPRINGDALE, AR N475JN Incident substantial
The failure of the right main landing gear torque tube support bracket/pivot bearing which resulted in the failure of the landing gear locking mechani…

The failure of the right main landing gear torque tube support bracket/pivot bearing which resulted in the failure of the landing gear locking mechanism.

Feb 15, 1999 PHOENIX, AZ N1557T Incident substantial The overload failure of the left main gear locking mechanism due to improper system rigging by maintenance personnel.
Sep 28, 1998 BURLEY, ID CGLHP Incident substantial A brake system failure for undetermined reasons. An intentional ground loop was a factor.
Jan 27, 1997 SPRINGFIELD, MO N414AM Incident substantial
the pilot's continued flight into known icing conditions with an inadequate windscreen deicing system and the diminished visual lookout. Factors were…

the pilot's continued flight into known icing conditions with an inadequate windscreen deicing system and the diminished visual lookout. Factors were the icing weather conditions and the windscreen ice.

May 27, 1996 BROOMFIELD, CO N414AW Incident substantial failure of the pilot to maintain adequate visual lookout by allowing his attention to be diverted.
Oct 27, 1995 GRT BARRINGTON, MA N2UD Incident substantial
the pilot's inadequate compensation for wind conditions, which resulted in an undershoot of the proper touchdown point for landing. Factors relating …

the pilot's inadequate compensation for wind conditions, which resulted in an undershoot of the proper touchdown point for landing. Factors relating to the accident were: the unfavorable wind conditions and the exposed runway lip.

Aug 30, 1993 DICKINSON, ND N36990 Incident minor the total failure of the airplane's heater system combustion air pressure safety switch.
Jul 30, 1993 LAKE CITY, FL N4232C Incident substantial
THE FAILURE OF THE PILOT-IN-COMMMAND TO PROPERLY FLARE BEFORE TOUCHDOWN AND THE PILOT'S DECISION TO LAND WITH EXCESSIVE AIRSPEED. A CONTRIBUTING FACTO…

THE FAILURE OF THE PILOT-IN-COMMMAND TO PROPERLY FLARE BEFORE TOUCHDOWN AND THE PILOT'S DECISION TO LAND WITH EXCESSIVE AIRSPEED. A CONTRIBUTING FACTOR WAS THE APREHENSION/ANXIETY OF THE PILOT DURING THE PRECAUTIONARY LANDING.

Jul 03, 1993 SEATTLE, WA N4735A Incident substantial
THE DISENGAGEMENT OF THE GEAR DOWN-LOCK MECHANISM DUE TO CORROSION AND THE PILOT'S INTENTIONAL OPERATION OF THE AIRCRAFT WITH KNOWN DEFICIENCIES IN EQ…

THE DISENGAGEMENT OF THE GEAR DOWN-LOCK MECHANISM DUE TO CORROSION AND THE PILOT'S INTENTIONAL OPERATION OF THE AIRCRAFT WITH KNOWN DEFICIENCIES IN EQUIPMENT.

Dec 19, 1992 REXBURG, ID N911AG Incident substantial THE PILOT DID NOT SELECT THE REMAINING FUEL SUPPLY. FACTORS INCLUDE A DETERIORATED FUEL SELECTOR VALVE.
Feb 13, 1992 LOGANSPORT, IN N4644G Incident substantial
THE PILOT'S FAILURE TO MAINTAIN AN ADEQUATE APPROACH SPEED WHICH RESULTED IN AN IMPROPER FLARE. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE INADEQU…

THE PILOT'S FAILURE TO MAINTAIN AN ADEQUATE APPROACH SPEED WHICH RESULTED IN AN IMPROPER FLARE. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE INADEQUATE INFLIGHT DEICING OF THE AIRFRAME SURFACES AND IN ICING CONDITIONS ENCOUNTERED.

Jan 19, 1992 GAYLORD, MI N6814R Incident substantial
DIRECTIONAL CONTROL WAS NOT MAINTAINED BY THE PILOT. FACTORS RELATED TO THE ACCIDENT WERE: AIRPORT SNOW REMOVAL HAD NOT BEEN PERFORMED BY THE AIRPORT …

DIRECTIONAL CONTROL WAS NOT MAINTAINED BY THE PILOT. FACTORS RELATED TO THE ACCIDENT WERE: AIRPORT SNOW REMOVAL HAD NOT BEEN PERFORMED BY THE AIRPORT PERSONNEL, A DARK NIGHT WITH FALLING SNOW AND THE SNOWBANK ON THE RUNWAY.

May 07, 1991 PIQUA, OH N222SV Incident substantial
THE PILOT'S INCOMPLETE PREFLIGHT OF THE FUEL QUANTITY AND THE INACCURATE FUEL GAGES, WHICH RESULTED IN FUEL STARVATION AND TOTAL LOSS OF ENGINE POWER …

THE PILOT'S INCOMPLETE PREFLIGHT OF THE FUEL QUANTITY AND THE INACCURATE FUEL GAGES, WHICH RESULTED IN FUEL STARVATION AND TOTAL LOSS OF ENGINE POWER AND SUBSEQUENT FORCED LANDING ON ROUGH TERRAIN. FACTORS RELATING TO THE ACCIDENT WERE THE PILOT'S IMPROPER INFLIGHT FUEL MANAGEMENT PROCEDURES AND HIS LACK OF EXPERIENCE IN THIS AIRPLANE.

Apr 06, 1991 AVENAL, CA N242AR Incident substantial
THE FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL AFTER STRIKING A DIRT BERM DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS THE FAIL…

THE FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL AFTER STRIKING A DIRT BERM DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS THE FAILURE OF THE PILOT TO ENSURE THAT THE AIRPORT WAS ADEQUATE FOR HIS INTENDED OPERATIONS.

Oct 17, 1990 JACKSON, WY N26853 Incident destroyed
THE PILOT'S INADEQUATE PREFLIGHT PREPARATION OF THE AIRCRAFT, HIS FAILURE TO REMOVE SNOW AND ICE FROM THE AIRCRAFT BEFORE TAKEOFF, AND HIS DELAY IN AT…

THE PILOT'S INADEQUATE PREFLIGHT PREPARATION OF THE AIRCRAFT, HIS FAILURE TO REMOVE SNOW AND ICE FROM THE AIRCRAFT BEFORE TAKEOFF, AND HIS DELAY IN ATTEMPTING TO ABORT THE TAKEOFF.

Mar 16, 1990 RAMONA, CA N711AG Incident destroyed
RIGHT MAIN GEAR SCISSORS ASSEMLBY BECOMING DISCONNECTED DURING LANDING ROLL, ALLOWING THE RIGHT RUN LANDING GEAR TO COLLAPSE; SCISSOR ASSEMBLY WASHERS…

RIGHT MAIN GEAR SCISSORS ASSEMLBY BECOMING DISCONNECTED DURING LANDING ROLL, ALLOWING THE RIGHT RUN LANDING GEAR TO COLLAPSE; SCISSOR ASSEMBLY WASHERS NOT BEING REPLACED AS RECOMMENDED IN CESSNA AIRCRAFT SERVICE BULLETIN ME83-37..

Dec 11, 1989 BULLHEAD CITY, AZ N8247Q Incident substantial THE PILOT'S FAILURE TO MAINTAIN SUFFICIENT CLEARANCE BETWEEN HIS AIRCRAFT AND GROUND OBJECTS DURING A TAXI TO THE RAMP AREA.
Dec 20, 1988 PONTIAC, MI N414CM Incident substantial Investigation pending
Jan 01, 1988 FAYETTEVILLE, AR N30ML Incident substantial Investigation pending
Jul 28, 1987 CUBA, NM N1648T Incident substantial Investigation pending
Jun 11, 1987 BINGHAMTON, NY N2691S Incident substantial Investigation pending
Dec 13, 1985 GEORGETOWN, DE N13FH Incident destroyed Investigation pending
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
← Cessna 414 For Sale All Cessna Models
Data source: NTSB Aviation Accident Database · About our data
View 41 Cessna 414 for sale ↓