Cessna 414 Safety Record

Complete NTSB accident and incident history. 149 events recorded from 1982 to 2026.

149

All Events

59

Incidents

15

Minor

16

Serious

58

Fatal (148 fatalities)

Date Location Reg# Severity Damage Probable Cause
Mar 19, 2004 Midland, TX N414FB Incident minor The in-flight wing fire for undetermined reasons.
Jan 31, 2004 Laupahoehoe, HI N5637C Fatal (3) destroyed
the pilot's disregard for an in-flight weather advisory, his likely encounter with marginal VFR or IMC weather conditions, his decision to continue fl…

the pilot's disregard for an in-flight weather advisory, his likely encounter with marginal VFR or IMC weather conditions, his decision to continue flight into those conditions, and failure to maintain an adequate terrain clearance altitude resulting in an in-flight collision with trees and mountainous terrain. A contributing factor was the pilot's failure to adhere to the VFR weather minimum procedures in the company's Operations Manual.

Dec 11, 2003 Greeneville, TN N1592T Fatal (4) destroyed
The pilot's failure to maintain airspeed while maneuvering in icing conditions on a circling approach for landing resulting in an inadvertent stall an…

The pilot's failure to maintain airspeed while maneuvering in icing conditions on a circling approach for landing resulting in an inadvertent stall and collision with trees and terrain. A factor in the accident was a partial loss of engine power due to the pilot's failure to activate the alternate induction air system, and exceeding the maximum landing weight of the airplane.

Jun 26, 2003 N. Fort Myers, FL N749AA Fatal (2) substantial
The failure of the pilot to maintain airspeed (Vs) following a total loss of engine power from the right engine due to fuel starvation, resulting in a…

The failure of the pilot to maintain airspeed (Vs) following a total loss of engine power from the right engine due to fuel starvation, resulting in an inadvertent stall, uncontrolled descent, and in-flight collision with trees and terrain. Factors in the accident was the failure pilot to feather the right propeller following the total loss of engine power, and his lack of total experience in the accident make/model of aircraft.

May 26, 2003 PORT JEFFERSON, NY N1234 Incident destroyed Loss of power to both engines for undetermined reasons.
Apr 10, 2003 Waleska, GA N822DB Fatal (1) destroyed The pilot's failure to maintain clearance from terrain.
Jan 14, 2003 Palm Springs, CA N127WW Serious (1) substantial
The flight instructor's improper selection of the high boost position for the operating right engine while on base leg to land, which resulted in a lo…

The flight instructor's improper selection of the high boost position for the operating right engine while on base leg to land, which resulted in a loss of engine power of the right engine. Factors associated with the accident are the left engine's loss of power for an undetermined reason, the flight instructor's failure to feather the propellers of the affected engines, and his failure to maintain directional control, which resulted in an off-airport forced landing.

Jan 06, 2002 Sturgis, MI N6560C Serious (1) substantial
the inadequate in-flight emergency planning/decision, the checklist not followed and excessive approach altitude by the pilot. Contributing factors w…

the inadequate in-flight emergency planning/decision, the checklist not followed and excessive approach altitude by the pilot. Contributing factors were the loose oil return line and weather.

Sep 29, 2001 Marshfield, WI N414NG Fatal (3) destroyed
The pilot's failure to maintain adequate airspeed (Vmc) which resulted in a loss of control. Contributing factors were the improper in-flight planni…

The pilot's failure to maintain adequate airspeed (Vmc) which resulted in a loss of control. Contributing factors were the improper in-flight planning/decision not to land at a closer airport and the lack of recent experience in multiengine airplanes by the pilot-in-command, the cylinder head separation, the inadequate manufacturing process, and the lack of continued airworthiness instructions relating to the Riley Super-8 STC.

Mar 28, 2001 Minneapolis, MN N8247Q Serious (1) substantial
The pilot not maintaining the proper airspeed during the circling approach, the inadvertent stall and the subsequent loss of control. Factors were th…

The pilot not maintaining the proper airspeed during the circling approach, the inadvertent stall and the subsequent loss of control. Factors were the pilot's decision to continue the approach in weather conditions below the approach/landing minimums, the continued flight below the minimum descent altitude, the pilot not following the approach airspeed listed in the owner's manual, the air traffic controllers not issuing weather information to the pilot, and the weather conditions.

Oct 17, 2000 KIEL-HOLTENAU, GE DIDIT Serious (1) Investigation pending
Jun 01, 2000 Prescott Valley, AZ N414PS Incident substantial
The pilot's physical impairment due to the cumulative effects of carbon monoxide from engine exhaust by-products, carbon monoxide from heavy tobacco u…

The pilot's physical impairment due to the cumulative effects of carbon monoxide from engine exhaust by-products, carbon monoxide from heavy tobacco use, and the loss of an undetermined amount of cabin pressurization. A factor in the loss of pressurization was a fractured clamp.

May 31, 2000 MONARCH, MT N5113G Fatal (3) destroyed
The failure of the pilot-in-command to ensure adequate airspeed for flight during a forced descent due to airframe icing, resulting in a stall. Facto…

The failure of the pilot-in-command to ensure adequate airspeed for flight during a forced descent due to airframe icing, resulting in a stall. Factors included: freezing rain conditions, airframe icing, an improper decision by the pilot-in-command to turn toward mountainous terrain (where a turn toward lower and level terrain was a viable option), mountainous terrain, and insufficient altitude available for stall recovery.

Jan 26, 2000 OKLAHOMA CITY, OK N7VS Minor substantial The failure of the pilot to deice the airplane prior to departure.
Dec 23, 1999 APODACA, MX XBEXF Fatal (2) destroyed Investigation pending
Aug 28, 1999 ALPINE, TX N67JM Minor destroyed
The pilot's improper use of the emergency fuel boost pump, which resulted in excessive fuel flow to the engine and subsequent total loss of left engin…

The pilot's improper use of the emergency fuel boost pump, which resulted in excessive fuel flow to the engine and subsequent total loss of left engine power. Factor's were the high density altitude, the pilot exceeding the airplane's weight and balance, the partial loss of left engine power as a result of the faulty magnetos, and the pilot's inadequate preflight inspection by not performing an engine run-up.

Aug 10, 1999 MONROVIA, LI N373BC Fatal (6) Investigation pending
Jun 13, 1999 SPRINGDALE, AR N475JN Incident substantial
The failure of the right main landing gear torque tube support bracket/pivot bearing which resulted in the failure of the landing gear locking mechani…

The failure of the right main landing gear torque tube support bracket/pivot bearing which resulted in the failure of the landing gear locking mechanism.

May 22, 1999 ORLAND, CA N8153Q Minor substantial A loss of engine power in both engines due to fuel contamination, which resulted from the fueling facilities improper quality control procedures.
Feb 15, 1999 PHOENIX, AZ N1557T Incident substantial The overload failure of the left main gear locking mechanism due to improper system rigging by maintenance personnel.
Nov 20, 1998 MATTAPOISETT, MA N6820J Fatal (1) destroyed
The pilot's failure to maintain control of the airplane after an undetermined failure of the airplane's attitude indicator. A factor in this accident…

The pilot's failure to maintain control of the airplane after an undetermined failure of the airplane's attitude indicator. A factor in this accident was fog.

Nov 18, 1998 MONROE, LA N30ML Serious (2) substantial The pilot's spatial disorientation which resulted in a loss of aircraft control. Factors were fog, low ceilings, and dark night conditions.
Sep 28, 1998 BURLEY, ID CGLHP Incident substantial A brake system failure for undetermined reasons. An intentional ground loop was a factor.
May 28, 1998 NORTH PLATTE, NE N888AA Minor destroyed
the slipped number two bearing in the airplane's right engine, which blocked the bearing's oil feed line, causing the bearing and the crankshaft to ov…

the slipped number two bearing in the airplane's right engine, which blocked the bearing's oil feed line, causing the bearing and the crankshaft to overheat and fracture. A factor contributing to this accident was the trees.

Dec 29, 1997 GUYTON, GA N414MT Fatal (2) destroyed
Inadequate maintenance of the cabin pressurization system, which resulted in inadequate pressurization and incapacitation of the pilot due to the hypo…

Inadequate maintenance of the cabin pressurization system, which resulted in inadequate pressurization and incapacitation of the pilot due to the hypoxia. Also causal was the pilot's failure to adequately monitor the cabin pressurization system.

Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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