Cessna 421C Safety Record
Complete NTSB accident and incident history. 136 events recorded from 1982 to 2024.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jan 08, 2024 | Carson City, NV | N421TP | Incident | substantial |
Airport personnel’s failure to properly prioritize their response actions, including updating the airport’s automated weather observation system recor…Airport personnel’s failure to properly prioritize their response actions, including updating the airport’s automated weather observation system recording in a timely manner to notify incoming pilots of a runway closure, which resulted in an airplane striking an immobilized airplane on the runway during landing at night. Contributing to the accident was the airport’s inadequate emergency response plan. |
| Dec 08, 2023 | McGregor, TX | N146TJ | Incident | substantial |
The failure of the spring pin in the right propeller governor, which precluded the pilot from controlling the propeller pitch to maintain engine rpm, …The failure of the spring pin in the right propeller governor, which precluded the pilot from controlling the propeller pitch to maintain engine rpm, resulting in a loss of engine thrust, excessive drag, and the subsequent forced landing to a field. |
| Apr 05, 2023 | Leesburg, VA | N880JS | Incident | substantial |
Separation of the left man landing gear scissor hardware, which resulted in a loss of directional control and subsequent runway excursion during landi…Separation of the left man landing gear scissor hardware, which resulted in a loss of directional control and subsequent runway excursion during landing. |
| May 15, 2022 | Monroe, LA | N619AC | Incident | substantial |
The failure of the maintenance personnel to properly reinstall the elevator trim tab hardware, which resulted in an in-flight separation of the elevat…The failure of the maintenance personnel to properly reinstall the elevator trim tab hardware, which resulted in an in-flight separation of the elevator. |
| Jan 07, 2017 | Jackson, CA | N71RC | Incident | substantial | The failure of the right main landing gear torque link bolt in overstress, which resulted in the collapse of the landing gear during the landing roll. |
| Apr 13, 2016 | Death Valley, CA | N21SG | Incident | substantial | A runway overrun for reasons that could not be determined based on the available information. |
| Mar 27, 2013 | Amarillo, TX | N805DC | Incident | substantial |
Maintenance personnel's failure to detect the misadjustment of the left landing gear actuator's switch after recent maintenance, which prevented the l…Maintenance personnel's failure to detect the misadjustment of the left landing gear actuator's switch after recent maintenance, which prevented the landing gear from locking in the extended position and resulted in the landing gear collapsing during landing. |
| Sep 11, 2012 | Kenedy, TX | N5534G | Incident | substantial | The pilot’s improper flare, which resulted in a hard landing and subsequent collapse of the landing gear. |
| Oct 30, 2008 | Mesa, AZ | N421PC | Incident | substantial | The failure of the hydraulic landing gear extension systems due to a ruptured line. |
| Apr 24, 2008 | Sterling, CO | N513FS | Incident | substantial | Failure and separation of the upper and lower right main gear torque links links, which resulted in a loss of directional control on landing roll-out. |
| May 22, 2007 | Kokomo, IN | N85SC | Incident | substantial |
The pilot not obtaining proper alignment with the runway during the emergency landing after takeoff, which imparted an excessive side load on the land…The pilot not obtaining proper alignment with the runway during the emergency landing after takeoff, which imparted an excessive side load on the landing gear. Factors contributing to the accident were the unstabilized approach and engine shutdown due to the oil leak. |
| Nov 26, 2006 | Moline, IL | N471BW | Incident | substantial |
The incorrect installation of the torque link scissor assembly by maintenance personnel, which resulted in the collapse of the right main landing gear…The incorrect installation of the torque link scissor assembly by maintenance personnel, which resulted in the collapse of the right main landing gear during landing. |
| Feb 18, 2006 | Indianapolis, IN | N98507 | Incident | substantial |
The main landing gear malfunctioned and failed to extend during the landing approach for an undetermined reason, which resulted in a main gear up land…The main landing gear malfunctioned and failed to extend during the landing approach for an undetermined reason, which resulted in a main gear up landing. |
| Aug 21, 2005 | Readington, NJ | N6159X | Incident | substantial | An encounter with animals during the landing - flare/touchdown. |
| Jan 19, 2005 | Muncie, IN | N421HG | Incident | substantial |
The inadequate flare and the directional control not maintained/obtained by the pilot. Contributing factors were the instrument meteorological condit…The inadequate flare and the directional control not maintained/obtained by the pilot. Contributing factors were the instrument meteorological conditions, the icing conditions, the limited visibility afforded by the windshield antiice/deice system, and the runway/approach lighting system. |
| Dec 21, 2004 | Henderson, TX | N369RK | Incident | substantial | The failure of the nose landing gear trunnion lug. A contributing factor was the non-compliance of the service bulletin by maintenance personnel. |
| Jan 03, 2004 | Window Rock, AZ | N911EA | Incident | substantial |
the pilot's failure to maintain adequate airspeed in the landing flare to compensate for airframe icing, which resulted in a premature stall and hard …the pilot's failure to maintain adequate airspeed in the landing flare to compensate for airframe icing, which resulted in a premature stall and hard landing. The degraded aircraft performance due to airframe ice was a contributing factor. |
| Mar 05, 2003 | Crescent City, CA | N26533 | Incident | substantial |
The separation of the upper and lower right main landing gear scissor links due to improper maintenance, which resulted in a ground loop, and the coll…The separation of the upper and lower right main landing gear scissor links due to improper maintenance, which resulted in a ground loop, and the collapse of the right main landing gear during the landing roll. |
| Feb 16, 2003 | San Francisco, CA | N321FL | Incident | substantial | The vehicle driver's inadequate visual lookout and failure to follow established procedures. A contributing factor was the dark nighttime condition. |
| Apr 25, 2002 | Tampa, FL | N237SM | Incident | substantial |
the fracture of the landing gear upper barrel due to fatigue cracking, caused by improper machining after the barrel was assembled during the manufact…the fracture of the landing gear upper barrel due to fatigue cracking, caused by improper machining after the barrel was assembled during the manufacturing process, resulting in damage to the airplane. |
| Mar 02, 2002 | Hailey, ID | N421DG | Incident | substantial |
Water contamination within the aircraft's landing gear hydraulic line(s) which froze and blocked the line(s) preventing extension of the right main ge…Water contamination within the aircraft's landing gear hydraulic line(s) which froze and blocked the line(s) preventing extension of the right main gear. A factor was the below freezing environmental conditions which the aircraft was operating in prior to and during the approach and landing. |
| May 29, 2001 | Greenville, MS | N51ER | Incident | substantial |
The improper installation by maintenance personnel of the push-pull rod assembly on the right elevator trim tab horn resulted in an in-flight separati…The improper installation by maintenance personnel of the push-pull rod assembly on the right elevator trim tab horn resulted in an in-flight separation of the right elevator trim tab. |
| Dec 11, 1999 | GILLETTE, WY | N3912C | Incident | substantial | The collision with a deer on the runway during a night landing. A factor was the dark night. |
| Apr 21, 1997 | PIERRE, SD | N283PT | Incident | substantial |
the pilot's inadvertent activation of the number one throttle/power control. Factors were: the pilot left the cockpit unattended with the engines run…the pilot's inadvertent activation of the number one throttle/power control. Factors were: the pilot left the cockpit unattended with the engines running and a wet ramp. |
| Feb 06, 1997 | CEDAR CITY, UT | N45MV | Incident | substantial |
water contamination in the hydraulic system, which froze in the (right) main gear hydraulic actuator, and restricted movement of the (right) main gear…water contamination in the hydraulic system, which froze in the (right) main gear hydraulic actuator, and restricted movement of the (right) main gear retraction and extension system. |